but couldn’t get it to run. The error I’m getting is:
** ERROR: main:565: Failed to set pipeline to PAUSED
Quitting
ERROR from src_bin_muxer: Output width not set
Debug info: gstnvstreammux.c(1616): gst_nvstreammux_change_state (): /GstPipeline:pipeline/GstBin:multi_src_bin/GstNvStreamMux:src_bin_muxer
App run failed
Eagerly awaiting a response on it. Thanks for reading.
Our internal team has implemented a change of nvyolo plugin for deepstream-app.
It will be released soon after testing. It’s recommended to wait for the official update.
Yes, I am aware of that. I thought I might as well try as there was nothing else I could find. Thanks for your reply. Looking forward to the official update.
Hi, I have the same Error using Jetson.
** ERROR: main:655: Failed to set pipeline to PAUSED Quitting
ERROR from src_bin_muxer: Output width not set
Debug info: /dvs/git/dirty/git-master_linux/deepstream/sdk/src/gst-plugins/gst-nvmultistream/gstnvstreammux.c(2283): gst_nvstreammux_change_state (): /GstPipeline:pipeline/GstBin:multi_src_bin/GstNvStreamMux:src_bin_muxer
App run failed
I tried to run ObjectDetector_Yolo.
Please I need Help.
I am having the same issue also on a Jetson Nano. Could you tell me how you fixed it? Probably easier than opening a new topic and waiting for response…